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by WarmWash
57 days ago
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Yes, but we are splitting hairs at that point. The transient spike is a high impedance voltage that is tripping the high impedance internal protection circuitry of the magnetometer. So whether we have 20mOhms of capacitive decoupling or 500mOhms of inductive decoupling, both are better than the infinite impedance of nothing there. We're not building a precision filter, were cutting the paws off of a paper tiger. No need to let perfect be the enemy of good. |
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So from my perspective, increasing the capacitance from 22uF on that output line to 22.1uF with a 100nF cap will likely do jack diddly shit.
It is far more likely that, ex, the author of this post screwed up the regulator design. Ex: did the author mistakenly think that more capacitance is better-er and stick a 100uF cap there, blowing out the phase margin of the feedback of the switching regulator?
Was the inductor properly sized? Not just inductance but also saturation current and internal resistance?