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by cmurf
2607 days ago
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Overspeed is the result of the mistrim. They were in fact flying the plane, the significant back pressure they used to fight the mistrim makes that clear. On what basis do they anticipate 4 seconds after two successful nose up trim using yoke toggle switches (manually initiated, electric motor turns jackscrew) that MCAS will cause a 40 degree nose down within seconds? Nothing. There's no basis for expecting such madness. The emergency AD following LNI610 doesn't at all account for significant mistrim, the possibility of heavy jackscrew loading forces that could prevent manual (handcrank) retrim, and the necessity of setting stab trim switches back to normal to solve the mistrim. It's realy vile to me that this whole mistrim scenario was not thoroughly explored by the FAA and NTSB (independently of each other) in 737 MAX capable simulators following Lion Air 610. Very clearly the emergency AD was still inadequate months after Lion Air 610. Could ET302 have been prevented? Perhaps, but not based on the then published AD. |
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No, it wasn't. Overspeed was because the pilots basically firewalled the throttles and never once touched them. Look at the Lion Air flights, they never came close to those sorts of speeds.